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Cetus3d z banding
Cetus3d z banding






cetus3d z banding
  1. Cetus3d z banding install#
  2. Cetus3d z banding pro#
  3. Cetus3d z banding download#

To perform this upgrade, you will need the following hardware:Ĥ80mm (48cm) GT2 Timing Belt, 6mm wide with 2mm pitchġx 16T GT2 bearing idler pulley for 3mm shaftīefore starting this project, go to our thingiverse page and download and print out the printed components associated with this project. (Optional Clip-On Fan Shroud part from our Zero-Offset E3D Adapter) (Optional X-Axis Idler Pulley Alignment Clip) The 3D printable files for this project can be found at the following links:

Cetus3d z banding install#

The X-Axis belt and pulleys will need to be replaced, and you will likely want to install fresh LM6LUU bearings on the new carriage, to obtain a smoother operation than stock, and avoid having to extract the existing bearings from the stock carriage. It is hard to mount the rods perfectly with the couplers, a little misalignment and one introduces wobble (X/Y wiggle).Īnyway, M6 gives slightly higher resolution in Z axis with 0.005mm per motor step.The purpose of this modification is to completely replace the stock Monoprice Select Mini V1/V2 X-Axis Carriage with a 3D printed replacement part, which will serve as a E3Dv6 compatible hot-end mount, but will also feature an integrated belt attachment and tensioning system for a GT2 timing belt. wobble seems mostly introduced by the couplers (either printed or PVC pipe):.less wobble, but still wobble despite of “straight” M6 threaded rods.

cetus3d z banding

Cetus3d z banding pro#

I made a small package Geeetech / CTC DIY I3 Pro B M6 Z Axis Conversion to use M6 threaded rods instead of M8. Recommendation: print the mounts, print the two bearings, and print the XYZ Calibration Cube or whatever reference item, and see yourself which option works better for you.

cetus3d z banding cetus3d z banding

What I noticed was, once I used the printable bearings for a print, and removed it, the threaded rods wobble already less – but as said, best results I achieved with no bearing and wide floating ends or with the tight bearings. whether left and right go the same way or cancel each other wobble out. I would also guess, the unevenness of the threaded rods and their position to each other also matters, e.g. 1-2mm play.īest results I achieved with floating ends or with tight bearing – in other words, either leave it open or make it stay close, but worst is to give it a little play and threaded rods will show their unevenness on the prints. Worst Z wobble was with original Z mount with ~4mm play or the loose bearing with apprx. You may print two bearings (OD 22mm, ID 8mm), make sure to test inner diameter, so the threaded rod slides smoothly – if required use a 8mm drill to widen the inner hole. The new Z bracket provides more space for the threaded M8 rods than the original wooden bracket: The issue isn’t simple: with or without fixation gives good results, some fixation gives more bad print results. Giving it some space on the top means the inherent wobble of the rod is distributed between top and X gantry – giving wobble artifacts on the print. Which means, either give it a lot of space so the upper end of the Z threaded rods can float, and thereby the X gantry can stay fixed (and not wobble) – or – fix the threaded rods and suppress wobble (there is still wobble but restricted).

  • original bracket: worst wobble of all, Z edge wobbly.
  • loose bearings: noticeable artifacts / wobble, Z edge wobbly.
  • tight bearings: gives very good surface, slightly worse than with no bearings.
  • no bearings / open floating: gives the smoothest surface, most straight Z edge.
  • Now comes the surprise, the best surface (best to worst):
  • new Z bracket with printed bearings (tight tolerance).
  • new Z bracket with printed bearings (with loose tolerance).
  • new Z bracket without printed bearing, apprx.
  • New Z bracket mounts (black), without/with printed bearing (white):
  • printable bearing added to restrict end (optional).
  • bearing hole widened to have more floating.
  • changed structural holes (larger hole -> smaller holes).
  • I hesitated to use lead screws due decrease of resolution (M8: 1 cycle = 1.25mm height, lead screw like TR8x8 (8mm dia, 4 starts, 2mm pitch, 8mm lead => 1 cycle = 8mm height) but otherwise gaining pretty straight lead.Īnyway, I searched Thingiverse for Z mounts for the CTC DIY and found a few, and adapted one design and made a remix Geeetech / CTC Prusa i3 DIY – Z Axis Bracket Remix with printable Bearing : Using a low-cost 3D printer like CTC DIY I3 Pro B (Geeetech I3 Pro B clone) with M8 threaded rods as Z axis with loose or floating ends is what you get – and so also some wobble or banding on the X axis due slightly bent M8 threaded rods – they barely come straight.








    Cetus3d z banding